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Other stuff that has been done is chase down the leak in the inlet manifold and seal the exhaust. Whist i had the manifold off the car i fitted non waxstat jets to the carburetters. This was not entirely easy as i had to modify the linkages slightly. All went together easily but i still have a high idle speed, looks like throttle spindles are next on the list.
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As well as this i used the opportunity to fit the 02 sensor to the exhaust manifold, the gauge now works and without to much fiddling i now now that at idle the car puts out %3.0 Co and is slightly lean on full throttle. I will leave well alone until after the cars MOT and then tweak some more.
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The last news is that i bought engine and radiator valances off an Ebay seller, it was spur of the moment but at least it one job i can now finish. The radiator valances i have made will be put on ebay once finished.
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